ssgunny
Registered
Instead of leaving it be I wanted to remove the PAIR pump braket. You have to remove the 2 crankcase bolts in order to do that. After removal I snapped one of the bolts while torquing it down. The pilot hole for the ez-out started a bit off center and when completed it is evident that it drilled at a slight angle towards the threads. I attempted the ez-out for several hours even thought the pilot hole was the way it was and had no luck.
It looks like I will have to take it to a machine shop and even if they are able to get it out I am not sure if the seal has not been compromised due to over torquing.
It looks like I will have to take it to a machine shop and even if they are able to get it out I am not sure if the seal has not been compromised due to over torquing.