That Honda looks like it's brand new...Parts run down . 1964 Honda 305 cc largest of it's time from Honda. View attachment 1635588View attachment 1635589View attachment 1635590View attachment 1635588View attachment 1635589View attachment 1635590
It was amazing . Entire sales team took a photo with it . Notice the hand crank on the bars for old time steering damper .That Honda looks like it's brand new...
My brother's '78 RT has one of those...and his throttle bar end cranks in to put tension on the throttle as a form or cruise control...It was amazing . Entire sales team took a photo with it . Notice the hand crank on the bars for old time steering damper .
Yup... that’s rich.Taco day!!! Love some tacos, sadly can’t eat them till this tooth is fixed. I know the rpms are up some with the +2. The biggest problem I see while riding and watching the afr is 10.2-11.5 ish range. Was 1/2 tank fuel for those 65 miles
Brian the young man seen in phots ( not me ) figured that on his own .Genius with the funnel attachment
Yessir. I will be having rob tune it here soon. I have all the connections setup in the tail for easy access. The pc3 has a 6ft usb cord already attached and the ecu has a boost by smith pig tail pre wired for flashing that.Yup... that’s rich.
Are you getting Rob to tune it?
Johnny on the spot with all the help!!! Good deal brother. That’s what parts of being a motorcycle community is all about. Helping others. So who came up with the funnel idea? I never thought of doing that to get into smaller places.Brian the young man seen in phots ( not me ) figured that on his own .
So a little back story . I met Brian yesterday at the Triumph dealer . he was picking up his 2010 675 after a recall my brother found online @ Moto space garage . Brian brought it to Moto space 1st for a no start condition . Paul test a few things but found the recall so it was taken to dealer for that , and see if it corrected the no start issue . It did not correct the no start so he picked it up while I was there yesterday , and I introduced myself to Brian . Told him I had been contacted by my brother Paul about it .
So today I was @ Moto Space to blast some ZRX stuff , and Brian shows up to drop off the 675 , and rent a both for a bit . Paul had another customer ( WERA racer with race bike ) so he was booked . I decided to assist with my Triumph software from TUNE ECU , and my bluetooth OBDII scanner . Just 1 code for low temp sensor . Ran tests on all items in Tune ecu soft ware , and they passed so time to get dirty .
Water in Fuel , bad / old fuel , and cake topper Failed BMC air filter ! My guess is improper cleaner used that dissolved the the sealing glue around the filter media edges . It all came apart as you can see .
With in an hour I got the old girl to Start . So now some replacement parts are on order , and he should be riding again in a few weeks .
The young Engineer Brian ( owner of 675 holding failed filter )Johnny on the spot with all the help!!! Good deal brother. That’s what parts of being a motorcycle community is all about. Helping others. So who came up with the funnel idea? I never thought of doing that to get into smaller places.
Very cool.Brian the young man seen in phots ( not me ) figured that on his own .
So a little back story . I met Brian yesterday at the Triumph dealer . he was picking up his 2010 675 after a recall my brother found online @ Moto space garage . Brian brought it to Moto space 1st for a no start condition . Paul test a few things but found the recall so it was taken to dealer for that , and see if it corrected the no start issue . It did not correct the no start so he picked it up while I was there yesterday , and I introduced myself to Brian . Told him I had been contacted by my brother Paul about it .
So today I was @ Moto Space to blast some ZRX stuff , and Brian shows up to drop off the 675 , and rent a both for a bit . Paul had another customer ( WERA racer with race bike ) so he was booked . I decided to assist with my Triumph software from TUNE ECU , and my bluetooth OBDII scanner . Just 1 code for low temp sensor . Ran tests on all items in Tune ecu soft ware , and they passed so time to get dirty .
Water in Fuel , bad / old fuel , and cake topper Failed BMC air filter ! My guess is improper cleaner used that dissolved the the sealing glue around the filter media edges . It all came apart as you can see .
With in an hour I got the old girl to Start . So now some replacement parts are on order , and he should be riding again in a few weeks .
I see the shop foreman is overseeing the workshopOut getting RTV silicon for the zrx in the garage. Stop for early dinner. View attachment 1635680View attachment 1635681
....or the 4 legged security system....I see the shop foreman is overseeing the workshop